ABBREVIATED AVIATION ACCIDENT REPORT (AAAR)
Source
AAAR
1. Case Number
1a. Date of Accident
1b. Time
1c. Aircraft Serial Number
2a. Classification
2b. Category
20000424003
Apr 24 2000
0930
8900168
D
FLIGHT
3. Type of Aircraft
4. Period Of Day
5. No Acft Involved
6. Nearest Installation
CH47D
DAY
1
02955 - FT WAINWRIGHT (AIM), AK
7. Accident Location
a. On Post
b. On Airfield
d. ALASKA
8. Organization Involved in Accident
Unit
UIC7
UIC6
UIC5
UIC4
UIC3
UIC2
MACOM
Station
WHT7B0
WHT7AA
W0EBAA
W32FAA
02955
B CO
4/123AB
ARTSPBD
USARPAC
FT WAINWRIGHT (AIM), AK
9. Organization Accountable for Accident
WHT7B0
WHT7AA
W0EBAA
W32FAA
02955
B CO
4/123AB
ARTSPBD
USARPAC
FT WAINWRIGHT (AIM), AK
10. Estimated Accident Cost
a. Total Loss
b. Aircraft Damage
c. Man Hrs
d. Man Hrs Cost
e. Other Mil Damage
f. Civilian Damage
No
$3112
5
$80
$0
$0
g. Injury
h. Total This Aircraft
i. Total Accident
$0
$3192
$3192
11. General Data
a. Mission
S/M
b. Flight Plan
c. Data Recorder
S - SERVICE
SINGLE
VFR
d. Night Vision
e. Fire
f. Fluid Spillage
g. Field Training
NONE
12. Flight Data
a. Emergency
Duration
Phase of Operation
2.5
B - STATIONARY (ENGINE RUNNING)
AGL
KIAS
Weight
Overgross
32000
b. Termination
Duration
Phase of Operation
B - STATIONARY (ENGINE RUNNING)
AGL
KIAS
Weight
Overgross
13. Type Event
84 - Power Train
91 - Electrical System
-
14. Accident Cause Factors
Human Error
Material Failure
Environmental
NO
DEFINITE
NO
15. Summary
After hot refueling, the #2 normal engine beep failed to respond to normal inputs. The #2 emergency beep auto/manual switch was placed in the manual position to control the engine manually. The #2 n2 control box was replaced and the cannon plug was cleaned. No further incidents occurred.
16. COMPONENT AND PART FAILURE/MALFUNCTION DATA
Part Information
a. Nomenclature
c. Part Number
d. NSN
e. MFG Code
f. Part Serial No
CONTROL BOX
SYLZ75614
6110011834852
05624
g. Cause Failure
Functional Group
Material
Maintenance
Design
Manufacture
03 - ENGINE/POWER PLANT 19 - CONTROLS
DEFINITELY
80 - THROTTLE 90 - SYNCHRONIZED
Type Failure
Cause Failure
356 - LOW ENGINE POWER
-
572 - RPM TOO LOW
-
17. ENVIRONMENTAL
a. General
(1) IMC
(2) VMC
(3) Unknown
b. Environmental Conditions
1. Weather Conditions
2. Other Conditions
(a) Hail
(a) Animals
(b) Sleet
(b) Fowl
(c) Fog
(c) Surface
(d) Drizzle
(d) Noise
(e) Rain
(e) Chemicals
(f) Snow
(f) Radiation
(g) Lightning
(g) Glare
(h) Thunderstorm
(h) FOD
(i) Gusty Winds
(i) Temperature
(j) Freezing Rain
(j) Vibration
(k) Other
(k) Dust
c. Aircraft Icing
No Yes
d. Turbulence
No Yes
19. MOON ILLUMINATION DATA
a. Above Horizon
b. Visible
c. Degrees Above Horizon
d. Percent Illumination
e. Clock Position
No Yes
No Yes
20. WIRE STRIKE DATA
a. Wire Strike
b. WSPS Installed
c. WSPS Engaged
No Yes
No Yes
No Yes
d. WSPS Cut Wire
e. WSPS Functioned
f. Wires Struck
No Yes
No Yes
Number wires
0
Dia.(inches)
21. PERSONNEL DATA
22. IMPACT/PROTECTIVE/ESCAPE/SURVIVAL/RESCUE DATA
a. Aircraft Space Compromised
b. Escape/Survival Difficulties
c. Protective/Restraint Equip Functioned
No Yes
No Yes
No Yes
24. FINDINGS AND RECOMMENDATIONS
Findings
Not Reported
Recommendations
Not Reported